Cyl #1 was pulling timing and it was the only one with the plug not indexed, 2-4 are doing just fine, still have the NGK plugs as gave away the stock plugs. I ordered a bunch of plugs and found one so #1 was indexed thinking that might be the cure but it did not resolve the issue. I was going to order some stock plugs but thought this would fix it and the tuner thinks these plugs work just fine from the logs we are pulling.
I am going to go ahead and order stock plugs since it has been shown the NGK are not the correct fitment even though my other cylinders seem fine with them.
This was happening on 91 Octane but the tuner was working it out on 91 and seemed we were OK but then I switched to +- 102 Octane Torco and have not been able to add much more timing or boost as the issue is there now again.
I think I may have a weak injector or coil pack, seems it would more likely be injector causing the cyl to run lean....
I can check the coil pack easily enough, once I get the Mishi radiator installed and other mods I am doing right now, hope to finish today. I can swap plugs around at the same time or after.
Not sure about the injector, I have not found anything about swapping out DI ones, any help would be appreciated if I need to do this which it seems.
I am pretty sure it is not false knock as have carefully gone over everything externally what seems could cause it.
Mods:
Cyborg turbo
Catted DP, CPE, 3" flow all the way out
Real CAI, 3", MAF installed
Cobb engine mount, DIY trans mount (lots of motion there, SS has some parts I sent, hope he makes them available
Cobb AP, pro tune in progress.
And helpful recommendations would be greatly appreciated.
Thanks
Rick
I am going to go ahead and order stock plugs since it has been shown the NGK are not the correct fitment even though my other cylinders seem fine with them.
This was happening on 91 Octane but the tuner was working it out on 91 and seemed we were OK but then I switched to +- 102 Octane Torco and have not been able to add much more timing or boost as the issue is there now again.
I think I may have a weak injector or coil pack, seems it would more likely be injector causing the cyl to run lean....
I can check the coil pack easily enough, once I get the Mishi radiator installed and other mods I am doing right now, hope to finish today. I can swap plugs around at the same time or after.
Not sure about the injector, I have not found anything about swapping out DI ones, any help would be appreciated if I need to do this which it seems.
I am pretty sure it is not false knock as have carefully gone over everything externally what seems could cause it.
Mods:
Cyborg turbo
Catted DP, CPE, 3" flow all the way out
Real CAI, 3", MAF installed
Cobb engine mount, DIY trans mount (lots of motion there, SS has some parts I sent, hope he makes them available
Cobb AP, pro tune in progress.
And helpful recommendations would be greatly appreciated.
Thanks
Rick